SoCal methane leak was largest in U.S. history | February 29, 2016 Issue - Vol. 94 Issue 9 | Chemical & Engineering News
Volume 94 Issue 9 | Latest News
Web Date: February 25, 2016

SoCal methane leak was largest in U.S. history

Scientists begin quantifying the effects of the Aliso Canyon disaster
Department: Science & Technology
News Channels: Environmental SCENE, Analytical SCENE
Keywords: environment, methane leak, gas well, Aliso Canyon, CO2
Southern California Gas Company employees work on a relief well to stop the Aliso Canyon methane leak. The leak was permanently capped on Feb. 18.
Credit: SoCal Gas
A photograph of gas company workers at the site of a relief well in Southern California.
Southern California Gas Company employees work on a relief well to stop the Aliso Canyon methane leak. The leak was permanently capped on Feb. 18.
Credit: SoCal Gas

Engineers earlier this month finally capped the massive methane leak at the Aliso Canyon natural gas storage facility in Southern California. The leak had spewed the potent greenhouse gas into the atmosphere for more than three months.

Now scientists, engineers, and policy-makers are assessing the disaster’s ramifications, with one research team publishing a report that concludes the methane release was the largest in U.S. history (Science 2016, DOI: 10.1126/science.aaf2348).

The team, which was led by University of California, Davis, scientist Stephen Conley and UC Irvine chemistry professor Donald Blake, monitored methane emissions from the facility, both on ground and with aircraft.

Conley, also the team’s pilot, made 13 flights above the site from November to February, sampling methane levels, and quantifying the size of the plume with measurements of wind speed and direction at different altitudes.

According to the measurements, the facility leaked a total of 97,100 metric tons of methane into the atmosphere. In 2004, a larger amount of natural gas was released from an underground well in Moss Bluff, Texas. But less of that methane reached the atmosphere because the gas exploded, converting methane to the much less potent greenhouse gas, CO2.

The leak began last year on Oct. 23. Environmental scientists blame poor maintenance of aging infrastructure at the facility as the cause. The Southern California Gas Company, which owns the facility, struggled to cap the leak at first and had to drill a relief well 2,600 m below the surface. On Feb. 18, they finally stopped the leak by plugging it with cement.

As the facility spewed out natural gas, more than 11,000 people in the surrounding Porter Ranch area fled to motels and temporary housing. Many grew sick from odors from mercaptan and other compounds in the gas.

Residents are now beginning to return to their homes. “We expect air sampling data to show that no emissions are coming from the [facility], and we anticipate the odors will cease,” Jeffrey Gunzenhauser, interim health officer for Los Angeles County, said in a Feb. 18 statement.

The magnitude of this leak may spur some action from the state on methane emissions in general, says Timothy O’Connor, director of the Environmental Defense Fund’s (EDF) oil and gas program in California.

For example, the leak is pushing California agencies to consider more seriously the climate impact of methane emissions. Some agencies base the climate effects of methane on what it does over a 100-year period. Because methane is gradually converted to CO2, methane’s warming potential is only 28–35 times as high as that of CO2 over a 100-year period, compared with about 80 times as high over a 20-year period. Thus the 100-year calculation might underestimate the climate-changing potential of methane emissions.

Chemical & Engineering News
ISSN 0009-2347
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